Possible tuning issue...
Posted: Mon Nov 08, 2010 9:07 pm
Hope you all don't mind me putting this up here as well!
Hey guys,
So I've had this possible tuning issue for some time now. Basically, the symptoms are that at about 1/8 throttle (3k - 4k IIRC?), the bike sounds really boggy. You know that sound when the bike's starting to run out of gas (don't ask how I know)? That's kind of what I'm hearing. Once I'm past that throttle / rev range, she seems to be fine.
Here are my carb specs:
Main jets - 118 (DJ)
Needle clip - #5 (DJ)
Float height - 24mm
Pilot screws - 3.5 turns out (could maybe come out another 1/8 - 1/4 turn)
FWIW, the bike ran fine previously with these settings.
Here's what I have done:
Cleaned the tank
Replaced the fuel filter
Cleaned the carbs
*All jets soaked in carb cleaner, passageways sprayed and clear, etc.
Checked the air filter (K&N - clean)
Bench sync
Plug wires have been trimmed & caps re-seated
Caps are all within spec
Plugs are fine
Here's what I have yet to try:
Re-check float height
Double-check pilot circuit passages
Vacuum sync
Lastly - I'm fairly certain the valves need to be adjusted.
Regarding the valve adjustment, is it possible that the valves being too tight could cause this problem? Just today, I read a post from Reelrazor (Brutal Tooth's thread) that made me think that this might be a possibility.
Thanks fellas!
Brandon
Hey guys,
So I've had this possible tuning issue for some time now. Basically, the symptoms are that at about 1/8 throttle (3k - 4k IIRC?), the bike sounds really boggy. You know that sound when the bike's starting to run out of gas (don't ask how I know)? That's kind of what I'm hearing. Once I'm past that throttle / rev range, she seems to be fine.
Here are my carb specs:
Main jets - 118 (DJ)
Needle clip - #5 (DJ)
Float height - 24mm
Pilot screws - 3.5 turns out (could maybe come out another 1/8 - 1/4 turn)
FWIW, the bike ran fine previously with these settings.
Here's what I have done:
Cleaned the tank
Replaced the fuel filter
Cleaned the carbs
*All jets soaked in carb cleaner, passageways sprayed and clear, etc.
Checked the air filter (K&N - clean)
Bench sync
Plug wires have been trimmed & caps re-seated
Caps are all within spec
Plugs are fine
Here's what I have yet to try:
Re-check float height
Double-check pilot circuit passages
Vacuum sync
Lastly - I'm fairly certain the valves need to be adjusted.
Regarding the valve adjustment, is it possible that the valves being too tight could cause this problem? Just today, I read a post from Reelrazor (Brutal Tooth's thread) that made me think that this might be a possibility.
Thanks fellas!
Brandon